1.Main ignition done.
2.H2 taken whrn temp. reach to 550 Deg.
3.Cleaning section 1Def pinch roll damge to dryer high temp.So don’t run entry below 40 MPM.
4.Entry no-2 pinch leveller intermash not helthy.So setting adjustment done with mech and elect.Now under observation.
5.During startup of commercial coil pinch mark comes, because of spray pump filter clogging.
6.TR-2 discharging not healthy because of DD-2 pinch roll not going to down position.
7.For DOS A coil all conveyor and TR area cleaning work.
1. Delivery crop cut trial done at 60 mpm and 1 time sample got carried over.
2. Labeller information check NG alarm coming in every coil.
3. TR 2 EPC checked for OD shifting problem but not resolved.
4. Entry strip crop cut slip to lower pass from upper pass so stop the line and take out the scrap.
5. DOS A trial coils shifted to yard and temp packing done.
6. Zig zag winding problem in TR1 in wider width.
7. OD shifting problem in TR2 continue.
8. Tensile test sample of banding m/c sent to lab.
9. 1 time SCB ball discharging seq in AUTO mode NG but all conditions healthy. After that select semi auto and start seq. Inform to electrical for the problem.
10. Electrode wheel wear out after 14 welds only so change the electrode wheel.
1. TR 1 and TR 2 OD shifting and stagger winding problem, so mech. Maint changed the EPC main pressure line filter.
2. Scrap baller bucket empty.
3. Entry scrap bucket empty.
4. Center stops for 9 mins as single POR running and coil insert auto abnormal.
5. Entry section lower pass 1.9 thick crop was stuck at tilting table, so taken it out with the help of mech, single POR running from 3:30 am to 5:00 am.
6. OD shifting from TR 1 and TR 2.